A Holley carburetor is an impressive assemblage of 'kludges' (only from a fuel injection perspective, of course) that supplies fuel to an engine over a wide range of speed and load conditions. The choke provides a rich mixture during a cold start, and a fast idle cam keeps the engine running during its warm-up. Idle circuitry maintains an idle, and off-idle circuitry provides a transition to the main jets. An accelerator pump covers up the stumble that would otherwise occur when the gas pedal is pushed, and a power valve meters in extra fuel to help with detonation when the engine is under heavy load.
Model engines aren't typically loaded but they are expected to start, idle, and rev over a reasonable range including short pulls into w.o.t. Although the choke valve is currently my index finger, the new needle valve is providing good running settings for either idle, mid-range, or wide open throttle up to 4500 rpm. It can also provide a compromise setting for idle through midrange or for midrange through top-end. However, there's no setting that includes a 1k idle which was one of my goals for the engine.
A major limitation of a simple one needle carburetor stems from its Venturi being on the throttle. The Venturi discussions in the earlier carb design posts pertained to w.o.t. In mid-range though where the Venturi's geometry changes as the throttle is rotated toward idle its effective size becomes progressively smaller. Higher and higher velocity air draws more and more fuel from the spray bar, the floor drops out of the A/F ratio, and the engine dies.
An air bleed added to this simple style carburetor can extend its idle. An air bleed is an atmospherically vented hole that's cross-drilled through the throttle bore to intersect the Venturi as the throttle is rotated toward idle. When this hole is uncovered by the Venturi the additional air flowing through it tends to lean the mixture and extend the idle to a lower rpm than would otherwise be possible. The diameter of the hole is determined experimentally, but mine usually end up around 1/3 the diameter of the Venturi. The 289's vent hole has a sliding cover to fine tune the amount of air entering the bleed passage. Depending upon exactly how the hole intersects the Venturi, the additional air may also draw some fuel from the spray bar.
One of the photos is a cross-sectional rendering of the 289's carburetor showing the original air bleed being uncovered as the throttle is rotated closed. Tests with the vent hole fully covered and the needle valve adjusted for a midrange setting of 2500 rpm showed the engine stalling at about 1600 rpm as the throttle was decreased. With the vent hole fully open, the carb was able to reach a minimum idle of some 1450 rpm. Again the engine stalled when the vent hole was re-covered.
An identical second bleed hole intersecting the original atmospheric vent was drilled parallel and just above the original bleed hole. The total area of the two bleed holes is equal to that of the atmospheric vent. Repeating the test showed the minimum idle had moved down to about 1300 rpm while the vent hole was totally uncovered, and again engine died when the vent was covered.
Since testing showed the lowest idle always occurred with the vent hole completely uncovered, it's possible that more bleed would allow an even lower idle. Enlarging the bleeds and/or vent was too risky at this point though.
Drilling the bleed passage(s) to intersect the Venturi above the throttle's axis as shown in the two photos provides a slow transition to idle since the extra air also draws some extra fuel from the spray bar. Drilling a bleed hole from the opposite side of the throttle bore so it intersects the Venturi below the throttle's axis provides a more abrupt transition since less fuel will be drawn by its extra air. This third bleed is on my short list of modifications to try next.
A better flywheel (or in my case any flywheel) may allow a lower idle, and it should reduce some of the engine's annoying vibration. The starter clutch isn't a conventional Bendix-type mechanism that disconnects the starter from the flywheel while the engine is running. Instead, the starter is permanently engaged with the flywheel with a sprag clutch disengages the flywheel from the crankshaft while the engine is running. The result is that external to the engine there's no significant rotating mass on the crankshaft. Attending to this is the second thing on my to-do list.
In the meantime though ...
I've run nearly a quart of gasoline through the engine while playing and getting to know it. The top-end looks like it will be 4500 rpm which is 1500 rpm below the original HiPo's redline. This is pretty much what I had expected from the model's small intake valves and their less than optimum lift. I don't yet know if the CDI ignition is a limitation.
The engine has been burning an average of about half an ounce of gasoline per minute. The 3 oz fuel tank allows about six minutes of run time. I've done two six minute runs which included mostly mid-range and some w.o.t. run ups, but I wasn't comfortable with the resulting 175F exterior head temperatures. In both runs the coolant temperatures in the radiator matched the head temperatures. Most of the fuel was consumed with more comfortable three minute runs where the head and coolant temperatures reached 145F.
The PCV draft system that was designed to lubricate the top-end is working well. With the valve covers gasket'd to the heads, the valve train components accumulate an oil film, and oil collects on the valve covers under the vented filler caps.
The exhausts run cleanly with no smoke, and I recently removed and inspected the plugs, and their colors are very acceptable.
The engine seems to like 20 degrees BTDC at all rpms. In the process of playing with the timing I discovered the rotor tip electrode had been rubbing against the cap electrodes. By the time I'd discovered the fine brass debris inside the cap, the rotor had already lapped itself in. However I removed two thousandths from the tip for additional margin, and I'll revisit the timing later.
Other than its higher than desired idle, my biggest disappointment with the carburetion is that there's no single needle setting that includes both a cold start and reliable mid-to-high speed running. The engine takes nearly a minute to warm up to the where fuel atomization stabilizes, and during this time the needle must be fiddled with. My other (and smaller) engines heat up much quicker, and so the fiddling time is much less.
The plan is to next tackle the flywheel issue and to add an opposite-side bleed hole. - Terry