Hi Raygers, a suggestion:
If you can bury 3/4 of the tube array in DRY sand, in a bucket/tin, then you will only need half the heat on the top plate when soldering. I have a large coffee tin (2l/4 pints) that serves me well, but maybe you need a bigger one? At least 1 inch of sand beneath and all the way around. Or wrap the job in firebricks: See photos.
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These also show the use of "pre-heating" blowlamps, that do not get the silver solder to melt, but mean that when the main Propane torch is introduced to the joint, heat flow away from the joint is reduced making the time for making the solder flow properly is much shorter, and less time for the flux to burn. During pre-heat I use a lower temp flux, then add the higher temp flux when I introduce the Propane torch on the joint proper. After soldering, cover everything so it cools slowly, so differential cooling does not crack any joints! - I have experienced that repairing boilers, where I don't wrap it up, but quickly remove from the sand and air cool... The outside shell cools rapidly, compared to the tubes, and stresses the hotter tube joints, showing any weakness on the subsequent hydraulic test as a leak from a cracked joint! (I have heard a slight "ping!" when I think this happened). - I have made a lot of mistakes, and learned a lot from them.
I like the reinforcement around the Firehole. This is the weakest part of the whole boiler. Huge stress concentration factor at the penetration (3.3 seems to be the accepted Standard SCF). The inner firebox tube is actually in compression: boiler pressure trying to buckle the tube inwards especially at the point where the fire hole reinforcement meets the tube wall. From Thick reinforcement and metal overlap to thin wall of main tube surface needs a silver solder that gives a good fillet (1/8in 3mm), to reduce the SCF at the change of stiffness. - I use 55% silver for fillet making. - Expensive stuff! Also a difficult repair if it cracks and fails, And such a failure is a testament of the "poor design" - not workmanship from the few boilers I have seen. I.E. they are simply operated/tested at too high a pressure. Re-certified for a lower NWP and Safety relief pressure (and Hydraulic test pressure) means they do not fail later, following repair.
My calculations and research of Tech papers at this interface are all indicative of an SCF that is not considered by many designs... so the weak spot can fail a boiler in later life from fatigue, where thin inner firebox wall meets thick fire-hole reinforcement.
The only boiler I inherited to repair and been repaired a few times, due to fatigue from the high stresses - probably from the 2 x Hydraulic test, added to weekly steaming, at a pressure higher than my calculations said was OK. I should be interested in your calculations, if you feel you may want to share them? To learn from someone who has made a boiler like this. Other boilers for which I have produced calculations, to re-certify old boilers (From scratch, where the original design has been lost) have typically come up with a NWP of around 30psi, when the original appears to have been run at 60 or 80 psi, from the old pressure relief valve operation pressure. That would have meant the old operation was on a Safety factor of only 2 or 3, not the "8" of modern Regs. and Standards.
I have also dismantled a Marine/Cornish style boiler with cross tubes on a large firetube and seen where all the cross tube joints had failed, repeatedly, and been repaired repeatedly, when the boiler was operated in a boat at 45psi, or higher as it had been "rated" for 60psi NWP!! It was evident that the wall of the main firetube had deformed as it cracked and failed the joints to the cross tubes. A Design problem for the pressure selected! My calculations said a NWP between 12psi and 18psi would be OK (conservative to optimistic) but a higher NWP (45 to 60psi) would mean the 2 x Hydraulic test would deform the firetube at the stress concentration of the cross-tube joint. Most of the cross-tubes had repairs of Soft lead solder with LARGE fillets on the inside of the Fire-tube - the only area where the joints were accessible.
- I scrapped this firetube with cross-tubes and made a completely new fire-tube assembly. Even so, the new Firetube only has a NWP of 20psi as it is in Compression, with stress concentration factors at the end joints and compressive strength of annealed copper as the basis to the design calculations. (NOT the Tensile strength). Hence my curiosity about your design?
While I think my current boiler analysis is "Safe", it may be too conservative, or risky, so I am open for discussion if you want to privately send me calculations, or design support information on this?
I hope there is something useful in this?
Thanks,
K2