JCSteam
Well-Known Member
- Joined
- Nov 30, 2016
- Messages
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Hello everyone,
Firstly hope you all had a great Christmas and wish you all well for 2020.
I've been absent for a while and a lot has changed at home, a house move, new job, (again), hopefully a little more settled now. Anyhow onto the post.
I was lucky enough to aquire a 2" Durham and north yorkshire traction engine for a very modest sum, it is far from been built to an excellent standard. When I first got it I looked over it and then started to take measurements and look over the parts I have.
Lists of issues that have been found are as follows
• wheels not running true to axle bores
• timing belts stuck on wheels with evostick adhesive
• front axle was not correctly centred before machining, meaning axle ends have large flat spots on them.
• Front perch fork seems stiff in the perch bracket so may need lapping or remachining
• smokebox has been silver soldered internally to seal the smokebox
• chimney base on smokebox not centred, it was machined incorrectly then bodged
• smokebox doesn't fit on the boiler, as the front tube plate has bulged the outer shell where it has been tapped in before silver soldering.
• The hornplates don't measure parralel, on investigation this is because the sides of the outer Firebox aren't parralel, and slightly taper to the top.
• the castings for the axles and crankshaft need their bearings remachining as it was bored oversize to accommodate the above
• the rear wheels same as the fronts with timing belts stuck on and rims not running true to the bores.
So on reflection not quite so lucky.......
Having had the ME write up for sometime I have all the plans available and spured on the purchase of this miniature traction engine.
Having got moved into a new house I have an average sized garage which compared to the 6x4' rickety wooden shed is luxury. I will be setting the workshop up before continuing much further with this thread, however arrangements have already been made to have the boiler initially hydraulic tested to working pressure. This will ensure there are no leaks in tubes or the main soldered joints. Without over stressing the copper boiler, until it's time to conduct a full x2 Working pressure test after the modifications described below are completed.
If all goes well with this then I will proceed to try and rectify first the issues that lead from the boiler, the bulge in the tube plate, and skimming the mounting bushes on the sides of the boiler to half overall dimensions from the centre line of the boiler. This will mean the hornplates will be able to sit vertically instead of tapered. Then I can move onto sorting the other bits out.
After a conversation with another chap who has built a Durham, he said he had a spare unmachined cylinder casting. And the bonus bit he said I could have it if I could pick it up. Sadly we are at opposite ends of the country (uk) so it means I'll have to arrange a courier to collect it. But far cheaper than paying for the fuel or even paying for a new one at over £100. So my head has been thinking of how to machine it on the myford ML4 and I think I have an idea which will involve a fixture plate attached to the vertical slide (bought some more tooling too), and the casting bolted to this through tapped holes in the top of the cylinder for the regulator chest. I can then machine the rear face of the cylinder, the bore and the mounting all in one setting, turn the vertical slide around and machine the front cylinder face. Then mounting on an expanding mandrel on the vertical slide I will be able to machine the valve face and make any corrections to the valve ports if required.
Doing it this way will ensure that four of the five major machined surfaces will all be parralel to each other. Or at true 90° (for the cylinder ends).
Anyhow still paint to strip and a workshop to set up so will be back again soon with an update on how the hydraulic test goes.....
Firstly hope you all had a great Christmas and wish you all well for 2020.
I've been absent for a while and a lot has changed at home, a house move, new job, (again), hopefully a little more settled now. Anyhow onto the post.
I was lucky enough to aquire a 2" Durham and north yorkshire traction engine for a very modest sum, it is far from been built to an excellent standard. When I first got it I looked over it and then started to take measurements and look over the parts I have.
Lists of issues that have been found are as follows
• wheels not running true to axle bores
• timing belts stuck on wheels with evostick adhesive
• front axle was not correctly centred before machining, meaning axle ends have large flat spots on them.
• Front perch fork seems stiff in the perch bracket so may need lapping or remachining
• smokebox has been silver soldered internally to seal the smokebox
• chimney base on smokebox not centred, it was machined incorrectly then bodged
• smokebox doesn't fit on the boiler, as the front tube plate has bulged the outer shell where it has been tapped in before silver soldering.
• The hornplates don't measure parralel, on investigation this is because the sides of the outer Firebox aren't parralel, and slightly taper to the top.
• the castings for the axles and crankshaft need their bearings remachining as it was bored oversize to accommodate the above
• the rear wheels same as the fronts with timing belts stuck on and rims not running true to the bores.
So on reflection not quite so lucky.......
Having had the ME write up for sometime I have all the plans available and spured on the purchase of this miniature traction engine.
Having got moved into a new house I have an average sized garage which compared to the 6x4' rickety wooden shed is luxury. I will be setting the workshop up before continuing much further with this thread, however arrangements have already been made to have the boiler initially hydraulic tested to working pressure. This will ensure there are no leaks in tubes or the main soldered joints. Without over stressing the copper boiler, until it's time to conduct a full x2 Working pressure test after the modifications described below are completed.
If all goes well with this then I will proceed to try and rectify first the issues that lead from the boiler, the bulge in the tube plate, and skimming the mounting bushes on the sides of the boiler to half overall dimensions from the centre line of the boiler. This will mean the hornplates will be able to sit vertically instead of tapered. Then I can move onto sorting the other bits out.
After a conversation with another chap who has built a Durham, he said he had a spare unmachined cylinder casting. And the bonus bit he said I could have it if I could pick it up. Sadly we are at opposite ends of the country (uk) so it means I'll have to arrange a courier to collect it. But far cheaper than paying for the fuel or even paying for a new one at over £100. So my head has been thinking of how to machine it on the myford ML4 and I think I have an idea which will involve a fixture plate attached to the vertical slide (bought some more tooling too), and the casting bolted to this through tapped holes in the top of the cylinder for the regulator chest. I can then machine the rear face of the cylinder, the bore and the mounting all in one setting, turn the vertical slide around and machine the front cylinder face. Then mounting on an expanding mandrel on the vertical slide I will be able to machine the valve face and make any corrections to the valve ports if required.
Doing it this way will ensure that four of the five major machined surfaces will all be parralel to each other. Or at true 90° (for the cylinder ends).
Anyhow still paint to strip and a workshop to set up so will be back again soon with an update on how the hydraulic test goes.....