I have never liked to use the power feed on the mini lathe. It was noisy and it just didn't feel good. The saddle also did not move very smoothly towards the opposite end of the chuck, it jammed up against the lead screw. Because most of the work piece is short, I never used the entire 17" length bed and the lathe was left like this. Then one day I opened up the controller cover and saw the horrible screw thread that holds the pillow bearing which supports the lead screw. It was very crooked and once tighten, it bites on only one small, area of the bearing mount. The more you tighten the bolt, the more the mount moves away from the correct position and the lead screw becomes skewed or slanted. This is what caused the binding and that is also why so many mini lathe users experienced broken plastic gears.I stripped the entire mini lathe and re drill the holes. Once done, it was smooth and very quiet. The saddle could move the entire length of the bed easily. It was one difficult project to correct just 2 holes using Helicoil.