peatoluser
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- Apr 19, 2010
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I've always wanted a keats type vee block for the peatol , but commercial castings are just too big. But while trawling the archives i came across a 'sliding block faceplate' made by Marlyn Hadley and posted by oldmechthings and decided to try and make something similar for the peatol. so thanks gentlemen for the inspiration and sharing.
first step was to make the faceplate. marked out a 3 & 1/2 inch circle on some 5/16 by 4 flat bar and roughly hacksawed and filed to shape. then cut down one of those nose blanks and welded it roughly central to the plate. (didn't realise you could buy them. paid more for a local engineering firm to make me some :'( ).
screw onto spindle and make swarf. had to move on cross slide to so as to cover face and the O.D. was a bugger to do.
next was the slides. I was using 1 1/2 wide flat bar for the centre , so marked of as best i could the setting lines for it, drilled and bolted to face plate , then done the same for the outside guides. i used 4mm bolts but 5mm clearance holes for some waggle room.
out with the hacksaw and file , back on the face plate and scim O.D. once more. remove the centre piece and measure the two outside guides. Halve the difference and this is how much the centre slide is out of true with the faceplate. refit centre , loosen screws and tap all three in which ever direction corrects it, re tighten scim and repeat. I finally got a 2 thou difference and then realised this stage is unnecessary as i haven't made the vee fixture yet :
.
take out the centre piece and mill some slots in the faceplate
then thought of a modification and changed the centre bar for one with some overhang at either end. the vee block is just some BMS angle i bought thinking it was 90 degrees and could use it for some small angle plates. It isn't and has sat on the shelf mocking me for the past few months, but now i have a use for it! cut about 1 1/4 off it and tacked a small piece of scrap pipe to it.
chucked an off cut in the lathe and turned diameter true. made a clamp to bolt angle to this and faced off end
drilled and tapped centre bar for clamping bolts. also scibed 1 inch dia circle in centre and tapped 5mm. Make a setting washer from 1 inch bar 6mm hole about 1/4 thick. Bolt washer as best you can to fit circle, place vee against it and mark where the tube is .tap 5mm in centre of this tube . We need plenty of waggle room here.. I had to remake this bit as this hole interfered with the clamp hole. if i can make anything it sure is scrap :-[ . I've removed the washer in this photo
Refit bar to faceplate and screw onto lathe. Clamp a 1 dia. bar in vee block and then try and centre it , gentle taps with a small hammer - although at times i wanted to use a sledge hammer on the bugger ;
I settled for 0.003 TIR on the grounds i would be happy with that on a 3 jaw chuck.
all I've done is centre the vee on one dia, but we need the vee to be truly in line with the sliding member, if you get my drift. So, remove bar and refit washer making sure it is snug against the vee.
Now clamp a piece of ,say, 5/8 bar in the vee , move slide and centre this , trying not to disturb the washer. i.e. the vee should pivot on this . helps if you first get the for and aft readings from the slide the same before moving the vee.
go back and recheck with with the 1 inch bar that this setting hasn't shifted, well not by too much anyway.
Now its time to distorted all this accuracy. Weld the vee to the slide , and hacksaw off the tube and clean up.
we should have a nicely distorted base , so once again chuck a piece of bar, clean up the O.D., and clamp the vee to it. I also remade the clamp at this time. scim the base. once again I had to move the tool post to do this.
Not quite finished. reassemble on lathe , and again, centre up a piece of 1 inch dia. bar. this is going to be our reference dia. Remove and hacksaw the outer edges of the slide as close to the faceplate O.D. Rechuck and clean up O.D.
we now have a quick means of centering 1 dia bar. you can see why i changed the centre slider.
Doesit work?
turn O.D. of eccentric
offset and drill/ bore hole (its 0.150 inch offset in photo)
re centre using O.D. of faceplate and part off.
draw backs? I need to free off the slide a little to make setting the of-set easier, and now i suppose I'll have to try and build a triple expansion engine to justify making it ;D
Apologies for poor photos. cheap hand held camera. at least nobody can see my poor workmanship! I would ask for a decent one for Christmas, but apparently only my wife gets this privilege, i get what I'm given. anybody need spare socks, hankies etc?
happy swarf making, peter
first step was to make the faceplate. marked out a 3 & 1/2 inch circle on some 5/16 by 4 flat bar and roughly hacksawed and filed to shape. then cut down one of those nose blanks and welded it roughly central to the plate. (didn't realise you could buy them. paid more for a local engineering firm to make me some :'( ).

screw onto spindle and make swarf. had to move on cross slide to so as to cover face and the O.D. was a bugger to do.

next was the slides. I was using 1 1/2 wide flat bar for the centre , so marked of as best i could the setting lines for it, drilled and bolted to face plate , then done the same for the outside guides. i used 4mm bolts but 5mm clearance holes for some waggle room.

out with the hacksaw and file , back on the face plate and scim O.D. once more. remove the centre piece and measure the two outside guides. Halve the difference and this is how much the centre slide is out of true with the faceplate. refit centre , loosen screws and tap all three in which ever direction corrects it, re tighten scim and repeat. I finally got a 2 thou difference and then realised this stage is unnecessary as i haven't made the vee fixture yet :

take out the centre piece and mill some slots in the faceplate

then thought of a modification and changed the centre bar for one with some overhang at either end. the vee block is just some BMS angle i bought thinking it was 90 degrees and could use it for some small angle plates. It isn't and has sat on the shelf mocking me for the past few months, but now i have a use for it! cut about 1 1/4 off it and tacked a small piece of scrap pipe to it.
chucked an off cut in the lathe and turned diameter true. made a clamp to bolt angle to this and faced off end

drilled and tapped centre bar for clamping bolts. also scibed 1 inch dia circle in centre and tapped 5mm. Make a setting washer from 1 inch bar 6mm hole about 1/4 thick. Bolt washer as best you can to fit circle, place vee against it and mark where the tube is .tap 5mm in centre of this tube . We need plenty of waggle room here.. I had to remake this bit as this hole interfered with the clamp hole. if i can make anything it sure is scrap :-[ . I've removed the washer in this photo

Refit bar to faceplate and screw onto lathe. Clamp a 1 dia. bar in vee block and then try and centre it , gentle taps with a small hammer - although at times i wanted to use a sledge hammer on the bugger ;

I settled for 0.003 TIR on the grounds i would be happy with that on a 3 jaw chuck.
all I've done is centre the vee on one dia, but we need the vee to be truly in line with the sliding member, if you get my drift. So, remove bar and refit washer making sure it is snug against the vee.

Now clamp a piece of ,say, 5/8 bar in the vee , move slide and centre this , trying not to disturb the washer. i.e. the vee should pivot on this . helps if you first get the for and aft readings from the slide the same before moving the vee.

go back and recheck with with the 1 inch bar that this setting hasn't shifted, well not by too much anyway.
Now its time to distorted all this accuracy. Weld the vee to the slide , and hacksaw off the tube and clean up.
we should have a nicely distorted base , so once again chuck a piece of bar, clean up the O.D., and clamp the vee to it. I also remade the clamp at this time. scim the base. once again I had to move the tool post to do this.


Not quite finished. reassemble on lathe , and again, centre up a piece of 1 inch dia. bar. this is going to be our reference dia. Remove and hacksaw the outer edges of the slide as close to the faceplate O.D. Rechuck and clean up O.D.

we now have a quick means of centering 1 dia bar. you can see why i changed the centre slider.
Doesit work?
turn O.D. of eccentric

offset and drill/ bore hole (its 0.150 inch offset in photo)

re centre using O.D. of faceplate and part off.

draw backs? I need to free off the slide a little to make setting the of-set easier, and now i suppose I'll have to try and build a triple expansion engine to justify making it ;D
Apologies for poor photos. cheap hand held camera. at least nobody can see my poor workmanship! I would ask for a decent one for Christmas, but apparently only my wife gets this privilege, i get what I'm given. anybody need spare socks, hankies etc?
happy swarf making, peter